OTC 4868
Underwater Repairs Using Wet Welding in the North Sea
by M.B. Green, Occidental Petroleum (Caledonia) Ltd.
Copyright 1985 Offshore Technology Conference
This paper was presented at the 17th Annual OTC in Houston, Texas, May 6-9, 1985. The material is sUbject to correction by the author. Permission to
copy is restricted to an abstract of not more than 300 words.
SUMMARY
A description is given of the design and
installation of several wet welded repairs
made to appurtenances on 2 North Sea jackets.
Details are given of the mechanical propertieE
obtained for welds made in both the tank and
offshore.
Fatigue specimens were also prepared offshore
and subsequently tested in 4 point bending.
An S-N curve is developed and compared to
data available for welds made in air.
INTRODUCTION
Underwater repairs in the North Sea have
traditionally been made by either hyperbaric
welding or installation of mechanical/grouted
clamps. However, in the Gulf of Mexico wet
welding has also been used successfully.
Since several areas of secondary structural
significance required repair on the Claymore
platform's cathodic protection system it was
decided to make repairs by wet welding
prOVided it were demonstrat~d that adequate
mechanical properties could be developed from
such welds. The completion of these repairs
would permit evaluation of both the perform-
ance and cost of wet welds in a North Sea
application versus other methods of repair.
During the course of this repair work, furthex
defects were discovered to appurtenances on
the nearby Piper platform. The scope of
repair work was therefore extended to cover
these items.
BACKGROUND
The Piper and Claymore fields are situated
some 100 miles north east of Aberdeen in
Blocks 15/17 and 14/19 in the UK sector of the
North Sea. The Piper field was discovered in
January 1973 followed by Claymore in May 1974.
References and illustrations at end of paper
The Piper Platform is a 36 slot drilling and
production facility located in 474 ft
(144.475 m) water depth. It was launched in
June 1975 and initial production was achieved
in December 1976. Complete details of the
installation are given in a paper by
Duvivier and Henstock (1).
The Claymore platform is a 36 slot drilling
and production facility located in 360 ft
(108.728 m) water depth. The jacket is
conceptually similar to the Piper structure
except for the removal of one bay of framing
to accommodate the different water depth.
The jacket was launched in June 1976 and
first production was achieved in November
1977.
DESCRIPTION OF THE CLAYMORE PLATFORM REPAIRS
INTRODUCTION
Corrosion protection of the underwater
sections of the jacket was originally provide,
by an impressed current cathodic protection
system. 55 anodes were distributed over the
jacket terminating at various levels. Cables
to these anodes were run in pipes to the
surface, where they terminated in junction
boxes at the first level of jacket framing
above water. Cabling was then routed from
these junction boxes to the power supply
located within the topside modules.
The pipes or "anode risers" carrying the cablE
were welded to the jacket at each structural
member (either horizontal or diagonal) which
they passed. This connection consisted of a
cruciform plate fillet welded on both the
jacket member and "riser" sides (see Figure- 1)
There were 377 such connections distributed
over the depth of the jacket.
The anode riser was API 5L Grade B steel and
249
2 UNDERWATER REPAIRS USING WET WELDING IN THE NORTH SEA OTC 4868
1. Pump Casing PC 13 - A longitudinal
defect was reported from approximately
(-) 60 ft to (-) 70 ft.
In 1979 during grouting operations to
strengthen certain jacket members at the
(-) 40 ft elevation, cracks were discovered
in some jacket members at the anode riser 3.
supports. Initial remedial action consisted
of drilling 'crack stoppers' to prevent
propagation.
varied in diameter and wall thickness as
follows:
10.75" dia. x 0.438" from (+) 20'to(-)40'
8.625" dia. x 0.375" from (-) 40'to(-)100'
6.625" dia. x 0.375" below (-)100'
The cruciform plate was detailed as 0.375"
thick plate fromBS 4360 Grade 50D steel or
equivalent. However subsequent chemical
analysis of a sample taken from one of the
connections (46/10B 10) during the repair
operation showed the steel to be compatible
with the mild steel electrode (see Table 3) •
2. Shale Chute - Due to mud recirculation
problems with the original chute a
redundant anode riser had been adopted
to serve as a shale chute. This chute
had become blocked on one or two
occasions where it tapers from 10.75" to
6.625" diameter at (-) 120 ft. To
relieve these blockages it had been
necessary to cut the chute and introduce
a flexible coupling to connect the two
sections of chute. However, this
coupling had deteriorated to the point
where it needed replacement.
Anode Riser 23 - This is supported off
anode riser 18 "piggy-back" style.
Riser 23 had broken off above a support
at approximately (-) 10 ft.
This was followed by further inspection and
an engineering study to define the possible
cause and extent of the problem. Full
details of this work are given in a paper by
Nicholson et a1 (2).
In some instances cracks were restricted to
the 'riser side' of the connection only.
Considerable experience had already been
gained in the design and installation of
mechanical or grouted clamps (3 and 4) and
alternative methods of strengthening and
repair were constantly under review. Since
these particular cracks were not in primary
structural members it was decided to make
wet welded repairs in order to gain
experience of this technique from both the
aspects of time/cost and quality.
DESIGN OF REPAIRS
The connections selected for welded repair
are shown in Table 1. Design of the repairs
(5) was based on forces generated in the
computer model that had been used in the
earlier defect assessment study (2). One
location was selected for repair using a
small prefabricated habitat so that the
technique could be compared with the wet
welded solution for both cost and quality.
This "mini" habitat provided localised
shielding OL the repair area from the
surrounding environment without the usual
disadvantages of high cost and problems of
handling. Various alternative repair
configurations were also selected to permit
evaluation of their ease of installation and
subsequent performance. Details of the
various repair schemes and completed repairs
are shown in Figures 2 to 6.
DESCRIPTION OF THE PIPER PLATFORM REPAIRS
INTRODUCTION
Routine inspection on Piper had also found
significant damage to certain appurtenances
which appeared suitable for wet welded
repair. The items affected were:-
DESIGN OF REPAIRS
1. Pump Casing - Crack stopping holes were
drilled at the ends of the 'defect' to
prevent propagation. A mild steel
doubler plate was then fillet welded
over the defect (Figure 7). The
doubler plate was rolled to the correct
I.D. onshore.
2. Shale Chute - A transition piece was
detailed similar to the original design,
but made up in two sections to allow
ease of handling and installation
(Figure 8) • The transition pieces were
prefabricated onshore.
3. Anode Riser 23 - A replacement section
of riser and new support to riser 18
were made up using materials available
on the MSV 'Tharos" (Figure 9).
This particular repair illustrated the
versatility of wet welding since it had
taken only 10 days between first
discovering the damage to completion of the
repair.
A summary of the repairs is given in Table 2.
OFFSHORE OPERATIONS
INTRODUCTION
Sea Con undertook the wet welding as
nominated sub contractor to Wharton
Williams (2W) who were the main surface
diving contractor for the platforms. This
arrangement was used because the scope of the
wet welding work did not warrant a separate
contract with the inherent problem of split
responsibility.
A welding procedure qualification document
was prepared on the basis of the anode riser
pipe being API 5L Grade B and the cruciform
plates BS 4360 Grade 50 D steel. For the
proposed repairs it was unnecessary to obtain
welds with minimum notch toughness
250
TC 4868 M.B. Green 3
conforming to the Department of Energy's
Guidance Notes (8). However, a minimum
requirement of 25 ft Ibs average at (-) 20°C
was specified so that any procedure passing
this requirement could be subsequently
considered for more structurally significant
items.
MOBILISATION/DEMOBILISATION
accordance with AWS D3.6-83(6). The results
of these tests are given in Table 4. However
in the case of the wet welded specimens it was
believed that the water temperature in the
tank (80°F) could have a significant effect
on the results obtained. Furthermore,
conditions in the tanks, for both the wet and
habitat welding, would also be less severe
than those expected offshore.
FATIGUE TESTING
Further procedure plates were therefore
welded offshore at the actual work site and
subsequently tested. Results of these tests
are given in Table 5. However, because of
logistical and scheduling problems the
results of these tests were not used as a
basis for acceptance of the repairs.
In order to make a preliminary assessment of
the fatigue performance of wet welds versus
similar specimens welded in air twelve plate
specimens (Figure 10) were welded at (-) 40
ft. The steel was BS4360 Grade SOD and it
was welded in the 3G position. The specimens
were prepared with run on/run off plates on
either side of the weld.
The plates were tested under 4 point bending
(7) at a nominal stress ratio R = 0 (ratio of
minimum to maximum stress) • Loading was
applied using a servohydraulic actuator of
400 KN capacity. The load was measured
using an associated loadcell. The specimens
were supported in the test rig on rollers and
load applied through a spreader plate to
rollers at quarter points (Figure 11) •
ashore where the
removed by
The specimens were
in Figure 10.
The specimens were brought
run on/run off plates were
hacksawing and grinding.
then instrumented as shown
The mini habitat weld was undertaken by 2W
personnel during JUly 1984.
The wet welding team was mobilised to
Claymore on the 6th June 1984. The team
consisted of:-
The team was transferred from Claymore to
Piper on the 22nd June 1984. Demobilisation
from Piper occurred' on' 11th Jul-y.19 8.4 •
SITE PREPARATION
1 Diver/Welder Supervisor
1 Drilling Supervisor
4 Diver/Welders
1 Trainee
The wet welding contractor had expressed
concern regarding the effect of residual
magnetism on the welding process,
particularly as a result of the impressed
current system. Should the level of
residual magnetism exceed 40 gauss it had
been proposed that welding be suspended
until such time as the magnetic field
decayed to allowable levels by either
shutting down the cathodic protection system
and/or locally demagnetising the weld area
using local magnets. In the event it
proved unnecessary to shutdown the C.P.
system, although residual magnetism did
cause welding problems in several instances.
2W divers were used to clean the areas to be
repaired, drill crack stoppers if required,
and undertake initial fit up. Sea Con
completed final fit up.
WELDING
The wet welded repairs were made by Sea Con.
Mini habitat repairs were undertaken by 2W
divers. A complete breakdown of the times
required for each repair is given in Tables
1 and 2.
INSPECTION
The specimens were initially subjected to a
few cycles to ensure adequate 'shakedown' of
strain gauges. The strain gauges and crack
probes were calibrated and the specimens
sUbjected to fatigue loads at a frequency
between 5 Hz to 9 Hz depending on the level of
load. Continuous strain measurements and
crack probe measurements were maintained for
the duration of the test. Failure was
defined as the life at which the crack had
grown through 50% of the material thickness.
This failure coincided with the point at
which complete loss of specimen stiffness was
observed.
All welds were inspected 100% by 2W divers.
Welds made using mild steel electrodes were
inspected both Visually and by magnetic
particle.
Welds made using austenitic electrodes were
inspected visually only.
RESULTS OF PROCEDURE QUALIFICATION TESTS
Before proceeding with the offshore repairs,
procedure plates were welded in tanks onshore
and sUbjected to mechanical tests in
Results of the tests are given in Table 6.
Specimens 1 and 9 showed no signs of failing
after 2.14 million and 1.2 million cycles
respectively. They were designated "runners"
and the tests terminated.
~.linear regression analysis was performed on
the results (omitting the 2 runners) and the
resulting curve (Figure 12) compared with the
Department of Energy's 'F' curve (8) which had
been developed from testing of similar
specimens welded "in air" as part of the
United Kingdom Offshore Steels Research
251
UNDERWATER REPAIRS USING WET WELDING IN THE NORTH SEA OTC 4868
Project UKOSRP (9). The analysis of the the designer because of potential problems
data gave the following mean line equation with electrode compatibility.
for the wet welded Specimens:-
FUTURE DEVELOPMENTS
Loglo N = 12.592 - 3.1 Loglo Af
where N = cycles to failure The recent underwater welded repairs to Piper
A f = stress range (N/mm2) and Claymore have shown that both wet and
habitat welds can be made satisfactorily and
A statistical analysis of the data about the cost effectively. Because of constraints
mean line gave a standard deviation of of depth and welding position the use of
0.093; a design curve based on the mean austenitic electrodes for wet welded repairs
minus two standard deviations would is limited at present. Further development
therefore be defined by:- work on electrode make up is required to
improve workability, visual appearance and
Loglo N = 12.409 - 3.1 LogloAf mechanical properties.
CONCLUSIONS No mechanical or fatigue data was obtained
for the mild steel electrode during the
Mild steel electrodes have alrea”dy been used present project. Because .of the good
extensively in the Gulf of Mexico for wet workability and weld appearance achieved with
welded repairs. During the repairs this electrode, further work may be warranted
described here consistently good visual in obtaining this information. Also trials
quality was achieved and the integrity could be undertaken for welding of BS4360
confirmed by magnetic particle inspection. Grade SOD steel with a “modified” mild steel
This electrode did not suffer from the electrode.
positional constraints exhibited by the
austenitic electrode. ACKNOWLEDGEMENTS
The austenitic electrode used for welding This work was carried out as part of routine
the anode riser supports was difficult to repairs to the Piper and Claymore platforms.
work and generally had a poor appearance. The author is grateful to Occidental
Since subsequent magnetic particle Petroleum (Caledonia) Limited and their
inspection is impossible the poor visual Partners for permission to publish the result$
appearance of the weld may prove a hindrance of this work.
in assessing its subsequent performance.
Howeverr the fatigue strengths obtained REFERENCES
using this electrode (in 3G position) show
a good comparison with properties obtained 1. Duvivier S. and Henstock P.IL.
for similar welds made in air. “Installation of the Piled Foundations
and Production Modules on Occidental’s
Overhead .welding of butt welds (4G position) Piper ‘A’ Platform” Paper 8237
with the austenitic electrode proved Proceedings of the Institution of Civil
extremely difficult in the tank. Because of Engineers, London, August 1979.
this, every care was taken in the subsequent
design of repairs to eliminate any 2. Nicholson R., Cotter K.H. and Green M.B.
requirement for making butt welds in this “Defect Assessment of the Claymore ‘A’
position. However, the problems with Platform” Paper 356 Fourth International
making overhead butt welds may limit the Symposium on Offshore Mechanics and
scope for future repair design. Overhead Arctic Engineering, Dallas, February
fillet welds (4F position) do not present 1985.
the same problem and can be made to a
satisfactory quality. 3. Green M.B. “Experience with Fatigue
Analysis and Inspection Results in the
The application of mini-habitat welding North Sea” Paper OTC 4524, Offshore
proved successful in terms of both quality Technology Conference, Houston, May 1983.
and cost. Subsequent magnetic particle
inspection of the welds was possible and 4. Fern D.T. and Shear L. “Bolted Repair of
therefore the overall confidence level when Tubular Joints” Paper 23 Second
welding BS 4360 Grade 50D steel is higher International Symposium on Integrity of
than for a similar wet weld. Because of the Offshore Structures, Glasgow, July 1981.
time required for fit up of the habitat
(and its initial cost) habitat welds are more 5. “Underwater Welded Riser Repairs
expensive than equivalent wet welds and their Claymore ‘A’ Platform” Wimpey Offshore
use may be restricted to a “one off” Report WOL 122/83A, July 1983.
situation or where a higher confidence
level is required regarding quality. 6. American Welding Society “Specification
for Underwater Welding” ANSI/AWS D3.6-83.
It is important to obtain comprehensive
material documentation when making welded 7. “Testing of Underwater Wet Welded Plate
repairs. Any material substitutions (i.e. Specimens” Wimpey Offshore Report
use of high grade steels when a lower grade WOL 320/84, December 1984.
has been specified) must first be cleared with
%7
8. Offshore Installations: Guidance on
Design and Construction; U.K. Department
of Energy 3rd Edikion, April 1984.
9. “Background to New Fatigue Design
Guidance for Steel Welded Joints in
Offshore Structures” U.K. Department
of Energy, 1984.
TABLE 1
Claymore Platform Repairs
I I I I Approx. I
I / lApprox. Lengthl Welding {
I [ Depth I I Type of I of Weld I Time*
I Connection I (feet)! Type of Wpair [ Electrode I (inches) ~ (Hours) I
I I I I
I I
I 52/04B9 I 22 I Wet Weld I Austenitic I 120’’-3/8”FW I 12 I
I I I
I 5/9/0412 I 30 I Habitat Weld I AWS A5.1-691 149’’-3/8”FW [) 15 I
I I I Class E70181 75” - Butt !)
/ I I !
I 30/0452 I 30 I Wet Weld I Austenitic ~ ~7’’-8°8°FW ! ) 12 I
I I - Butt ~)
I II I I
I 46/10BIO I 100 ! Wet Weld I Mild Steel [ 40’’-3/8”FW I 5 I
I I I I I
I 47/10B12 I 100 I Wet Weld I Austenitic I 39’’-Butt I 5 I
I I I
NOTE: * Welding time is strictly on bottom time actually welding. It does
not include fit up, habitat installation (where appropriate) or
=pection.
FW = fillet weld
TABLE 2
Piper Platform Repairs
I I I I I Approx. I
lApprox. Lengthl Welding I
I Depth \ I Type of I of Weld Time* I
Item ~ (feet)~ Type of Repair I Electrode I (inches) \ (Hours) I
I I I
I I I I
I Pump Casing! 70 I Wet Weld [ MildSteel ~ 350’’-3/8”FW I 7 1
I PC13 I I I
I I I I I
I Shale Chutel 120 I Wet Weld [ Mild Steel I 87’’-3/8”FW I 7 I
I I I I I I
I I I Austenitic I 18” ) 1) I
I Anode Riserl 12 I Wet Weld )FwI)6 I
I AR23 I I Mild Steel I 18” ) ~) I
I /
NOTE : * Welding Time is “on bottom” time welding. It does not include prior
cleaning, fit up or inspection.
Fw = fillet weld
962
I
I
I
I
I
I M..,iptio”
1T.., IW.,”weld
P1.t.. ! [Plate, 1 & 2}
I mbitat ..ld
I (Plate 3)
I F. C19U. P1.t*.
~
clay - I AR 5/9/0412
-,. I (Ubit.t)
~ AR 30/0452
I
I AR 52/0489
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I AR 47/10B12
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I
I AR 46/LOB1O
I RW’air
I AR23
! P+lacemallt
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1111
I P1.t* I
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Grad. 50S I II I I 1
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,s4360 i 10 i 0.~6 ~ 0.37 j 1.36 j 0.015 \ 0.008 / 0.40 i 420 i SS0 i
Gr,ti 50. 1 1
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8s4360 ( 38 I 0.13 / 0.41~ 1.47 ~ 0.017 ~ 0.007 ~ 0.41 ~ 399 I
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